July 5, Sixty-Seven years Ago- the cause!
nw-mailing-list at nwhs.org
nw-mailing-list at nwhs.org
Sat Jul 8 22:08:23 EDT 2006
I knew you would come through Ed!
Thanks,
Charlie
-----Original Message-----
>From: nw-mailing-list at nwhs.org
>Sent: Jul 5, 2006 11:16 PM
>To: NW Mailing List <nw-mailing-list at nwhs.org>
>Subject: Re: July 5, Sixty-Seven years Ago
>
>Charlie - without lubrication, the boiler bearing slide wouldn't slide. It
>had worked after a fashion from Roanoke to Dry Branch but evidently siezed
>up at that point. After it made the little left curve at the end of Dry
>Branch Middle track, it wouldn't let the boiler come back to center; the
>front engine stayed skewed to the left. It's still skewed to the left in
>the photo. It stayed skewed to the left as the engine tried to make the
>right hand curve after the short straight.
>
>Again, get into the DOT special collections website and get report 2369.
>
>The engine was on its first trip after being taken out of storage. It would
>have been difficult to visibly detect the lack of lubrication, and nobody
>did detect it.
>
>I had heard that an A derailed in a yard (Williamson or Portsmouth) out on
>the west end due to the same thing, but I've never seen anything to confirm
>it.
>
>EdKing
>----- Original Message -----
>From: <nw-mailing-list at nwhs.org>
>To: "NW Mailing List" <nw-mailing-list at nwhs.org>
>Sent: Wednesday, July 05, 2006 12:18 AM
>Subject: Re: July 5, Sixty-Seven years Ago
>
>
>> Abramus:
>> Growing up in Radford, I had heard about this wreck from my dad for years
>> and this is the first photo I've ever seen of it. Thanks! He had family
>> that worked MOW along 'the river' through Belspring.
>> I had asked Ed King if he knew anything about it and he had a vague
>> remembrance of the incident. Now the question, to which I also posed to
>> Dr. Kiing, was the front engine uncooperative or did it sieze (bind) or
>> actually weld due to the build up of heat?
>> Charlie Long
>>
>>
>> -----Original Message-----
>>>From: nw-mailing-list at nwhs.org
>>>Sent: Jul 4, 2006 8:54 PM
>>>To: N&W Mailing List <nw-mailing-list at nwhs.org>
>>>Subject: July 5, Sixty-Seven years Ago
>>>
>>>It was sixty-seven years ago, July 5, 1939, that Engine 2030 turned over
>>>at Big Falls Cut on the Radford Division, due to a dry boiler slide.
>>>
>>>Attached is a photo.
>>>
>>>Keep your boiler slides well greased, boys !
>>>
>>>-- abram burnett
>>
>>
>>
>> ________________________________________
>> NW-Mailing-List at nwhs.org
>> To change your subscription go to
>> http://list.nwhs.org/mailman/options/nw-mailing-list
>>
>
>
>________________________________________
>NW-Mailing-List at nwhs.org
>To change your subscription go to
>http://list.nwhs.org/mailman/options/nw-mailing-list
More information about the NW-Mailing-List
mailing list